Go Back   Dallas Fort Worth 5.0 Mustang Club > Photos & Videos > Member's Rides


Sponsored Ads
Welcome to DFW50s.com

Register to remove these ads.




 
 
Thread Tools Display Modes
Prev Previous Post   Next Post Next
Old 10-14-2013, 10:24 AM   #1
Kaane
Member
 
Join Date: Jul 2013
Posts: 72
Default Kaane's 2013 Paxton Rebuild Thread

As a few of you heard, I blew up my motor couple days ago.

I was running e85 with BAP + stock fuel pump and it looks like it went lean during a 5th gear freeway pull. Lesson learned, stock fuel pump and boost on e85 don't mix. From the excessive oil burning and plug inspection, Number 8 piston has a broken ringland.

I was going to pick up the aluminator and sell my old motor, but that plan is toast.

Current plan:

Pull the motor, inspect for damage and send the block to MMR for their 1000hp rebuild. Heads should be ok, since I did not poke a hole in the block, I am hoping minor bore cleanup should be ok.

I will also buy a new return fuel system most likely fore dual 465's E85 ready.

I will also get a new clutch, most likely McLeod RST.

Here is the pic of the plugs, you can guess which is number 8.

Kaane is offline   Reply With Quote
 

Bookmarks




Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump